Production Optimization - Nashpa-4 Well

Source: www.gulfoilandgas.com 7/1/2024, Location: Asia

We are pleased to announce that Oil and Gas Development Company Limited (OGDCL) has successfully revitalized Nashpa-4 well. The well was re-evaluated for the potential of the upper zone of the Lockhart formation, resulting in an increase of 330 barrels per day (BBL/day) of oil and 7.7 million standard cubic feet per day (MMSCF/day) of gas at a wellhead flowing pressure (WHFP) of 1570 PSI. Additionally, 21 metric tons per day (MT/day) of LPG is being recovered. The gas is now being injected into the SNGPL network.

Nashpa-4 well is situated within the Nashpa Development and Production Lease (D&PL) in the Karak district of the Khyber Pakhtunkhwa province. Nashpa D&PL operates under a joint venture, wherein OGDCL as operator, possessing a 56.45% stake, alongside Pakistan Petroleum Limited (PPL) with a 28.55% share, and Government Holding Private Limited (GHPL) holds 15% share.

The above information is submitted in compliance of Section 96 of the Securities Act, 2015 and Clause 5.6.1(a) of PSX Regulations, for dissemination amongst your members please.


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